Project was to make the huge warehouse organized, improving productivity of UC operation
and reducing bin denials by 50% or more. Project Duration: 6 Months
Over and above,
the objective was to make space and accountability for New Parts and creation of
SOP’s to track KPI’s.
Typical results which could be achieved were: a) Reorganization of Interior Stores
of about 50,000 parts and packaging materials, b) Root cause analysis and onset
of Productivity Improvement in UC, c) Root cause analysis and reduction of bin denials
by about 50%, d) Work Place organization for better 5S through streamline material
flow, e)
Creating space and arrangements for proper storage and accounting of New
Parts, f) Creation of critical SOP’s etc.
Basic activities taken up were 5S, 3-Fixed & Visual Control, Introduction of 2-Bin
Concept, Flow Production system, FIFO etc., innovation in storage practices, planning
& monitoring activities etc.